Environmental Defense Institute
News on Environmental Health and Safety Issues
|
January 2008 |
Volume 19
Number 1 |
DOE’s Advanced Test Reactor Expert
Claims Errors
in His
Declaration to the Court
In January
2007, Keep Yellowstone Nuclear Free, Environmental Defense Institute, Mary
Woollen, John Peavey and Debra Stansell (“Plaintiffs”) filed a lawsuit against
the Department of Energy (DOE) for violations of the National Environmental
Policy Act (NEPA) for failure to conduct an Environmental Impact Statement for
the continued operation of the Idaho National Laboratory’s Advanced Test
Reactor (ATR).
On December 21, 2007, DOE’s expert
Robert Boston filed an “Errata” declaration to the court stating; “The
Plaintiffs have correctly pointed out that I made a mathematical error in my
prior declaration …” Boston goes on to state; “Such issues and
measures to change operations to extend the operating life have no relevance to
ATR, which identifies that neither the AELEX Program or the Life Extension
Program (LEP) have identified any significant aging related issues that require
upgrading to the ATR.” [1] In an earlier declaration to the court, Boston states the ATR, “heat exchangers
are in pristine condition.” [2]
The ATR went into service in 1969
(~40 years ago) and long past its original design life of 20 years. [3] DOE’s Life Extension Program is extending ATR
operations for another 35 years. Aging/degradation
of crucial ATR safety systems are well documented by Plaintiffs briefs to the
Court, and in DOE’s own reports. For instance, DOE’s 2005 ATR Facility
Certification Report shows:
a. Emergency reactor shutdowns due to
control rod failure and Emergency Fire Water System failures;
b. “Existing hardware has had
frequent failures and repair is uncertain with each failure, as there is no
current supplier of spare parts;”
c. DOE admits an “extensive NEPA
evaluation is required;”
d. “High Level Radiation Monitoring
System is not working;”
e. Primary reactor coolant heat
exchangers leak; Secondary heat exchangers are seriously corroded and “should
be replaced” because both “are operating beyond 200% of their 20-year design
life;”
f. Not all safety equipment qualified
to current seismic criteria;
g. Emergency water coolant pump
failure;
h. ATR non-compliant metal building
radiation confinement leaks “above the 125% acceptance line;”
i. On-site raw emergency reactor
coolant water supplies are not sufficient in ongoing commercial power outages;
j. ATR Vessel Vent Valves releases
radiation directly to the atmosphere during loss-of-coolant event;
k. ATR power level reduced from 250
MW to 150 MW due to core safety assurance problems;
l. Beryllium transuranic waste has
“no path to disposal” as required in regulations;
m. Liquid waste evaporator pond
liners are leaking;
n. Reactor Core Integral Change-outs
“failed two to four years after change-outs and are expected to fail two to
four years from now;”
o. During commercial power failure,
emergency diesel power generators failed to start;
p. Required National Fire Protection
inspection failed because fire dampers “were not made for inspection and some
dampers were installed backwards;” [4]
Leaks in the ATR Primary Heat
exchangers means radioactive contaminates are released to the Secondary Coolant
System and discharged to the atmosphere in the ATR cooling towers. "The M-85 [primary coolant system] PCS
heat exchanger developed a leak in the shell side. The leak was repaired, but
further investigation utilizing non-destructive examination indicated pitting
corrosion occurring in all the PSC heat exchangers. The
ATR PCS/ Secondary Coolant System (SCS) heat exchangers are operating beyond
200% of their 20-year design life." [5] [emphasis added]
As discussed below, in 2003 the ATR
released 1,180 curies to the atmosphere.
The ATR does not have the currently NRC required sealed radiation
containment dome structure otherwise required of commercial nuclear reactors.
The ATR Poses Grave Risks to Eastern Idaho and Western Wyoming
"The ATR is a Category A [the highest]
reactor with an operating power level of up to 250 MW, with potential for significant offsite radiological consequences. The ATR is classified as a Hazard Category 1
[the highest] nuclear facility in accordance with Department of Energy
standards for hazard classifications of nuclear facilities." [6]
Extending the operating life of the
ATR for decades into the future poses a major threat to public safety. The ATR
has no containment structure that would protect the public and the environment
in the event of a severe accident. It is housed in a thin metal-walled
building. As a result, according to the DOE, a severe loss of coolant
accident would release a “source term”
of 175,000,000 curies of radiation. [7] Such an accident, according to the DOE, would
result in a lethal dose of radiation for anyone within 19.4 kilometers of the
facility and would require the evacuation of areas within 105 kilometers of the
facility. This is an evacuation radius that would include all of Idaho Falls,
Rexburg, and Pocatello as well, an area with a population well in excess of
100,000. This potential accident at the ATR would be second only to Chernobyl
in severity.
Furthermore, this supposed
worst-case scenario assumes that the critical safety-related system relied upon
in the event of a Loss-of-Coolant-Accident (LOCA) the Emergency Firewater
Injection System or “EFIS,” will be fully operational and available, and will
pump water into the reactor confinement area to mitigate the effects of a LOCA.
[8]
However, as recent DOE safety
assessments have shown, the ATR/EFIS is badly flawed and may not operate properly.
It has suffered from design defects that hamper its operation, and moreover, is
seismically suspect, and may not operate at all in the event of a severe
seismic event at the facility. It could
result in a lethal dose of radiation for nearby INL workers and members of the
public, and would require the evacuation of a large area, disrupting the lives
of tens of thousands of people. Id.
Second, continuing to operate the
ATR without NEPA analysis will generate significant quantities of spent nuclear
fuel and irradiated transuranic beryllium waste, for which there is no
identified path for disposal. These wastes pose a substantial risk of
irreparable harm to human health and the environment and should not be
generated by the DOE without an approved plan for their safe disposal. Producing
more of this deadly waste, as the DOE does with each day of ATR operation,
creates a substantial risk of irreparable harm to the environment warranting an
injunction. The risk of irreparable harm is therefore sufficient evidence for
the court to issue an injunction.
DOE’s own previous Environmental
Impact Statements (EIS) state the ATR released 1,802 curies in 2000 and 1,180 curies
in 2003 to the atmosphere. [9] On average that is about 1,491 curies/year;
so over a seven year period 2000 through 2007 about 10,437 curies are released
to the air. These high emissions from
ATR suggest liquid waste is first sent to the ATR cooling towers w/o treatment
and the precipitates are then pumped to INTEC evaporators or the percolation
ponds. This represents a significant hazard
to INL workers and the downwind public.
In a four decade history of
operating the ATR formerly called the Test Reactor Area and currently called
the Reactor Test Complex the TRA/RTC DOE has dumped huge quantities (more than
85 billion gallons) of radioactive waste water into illegal, unlined
percolation ponds that resulted in massive groundwater contamination. [10]
Thus, the DOE should be enjoined
from continuing to operate the ATR until such time as it has (1) DOE completed
an Environmental Impact Statement and issued a record of decision on the ATR
Life Extension Plan; (2) DOE completed any and all “modernization” projects necessary
to ensure the safety of the facility for its extended lifetime; and (3) DOE
determined a path for safe disposal of the wastes the ATR will generate. [11] The following are related government reports
on ATR;
a. General Accounting Office report
states lax DOE enforcement program at its nuclear facilities;
b. DOE ATR Safety Analysis Report
acknowledges major problems in the primary coolant system. Problems with
emergency coolant and supporting structures, systems, and components were shown
to be worse than originally believed;
c. DOE Office of Facility Safety 2005
report states that "There is a potentially inadequate ATR safety analysis;"
d. ATR Loss of coolant accident
caused by either a seismic or other safety system failure has not been corrected
by substantive system upgrades;
e. Fuel cladding melting generates
fission product releases to the atmosphere. In 2003 the ATR released 1,180
curies to the atmosphere;
DOE ATR Safety Analysis Report still
only reviews a 3 inch break in the primary coolant system as the boundary. The
reliability of the two primary coolant pumps, (i.e. M-11 pump) has an
"uncertain" flow- rate. DOE reports "challenge the basis for
reliable on-site long-term water inventory for the Emergency Firewater
Injection System following a seismic event. On-site raw water supplies however
are not sufficient to last until commercial power could be reasonably assumed
to be restored. Therefore, uninterrupted
EFIA delivery to the ATR vessel was not ensured following a seismically induced
Loss-of-Coolant Accident."
Update on KYNF/EDI Freedom of Information Act Suit Against DOE
Wyoming Federal District Court Judge
Downes has scheduled his in-camera review of our requested FOIA documents
(related to the ATR) in Idaho Falls 1/22/08 through completion.
Only the judge, his staff, and DOE's
Robert Boston and Joel Trent will be present in this exparte review with
Mark Sullivan available only by phone if needed.
The purpose of this review is to
give Downes a concrete basis on how to rule on DOE's claim that these documents
must be exempt (for national security reasons) from release under our
FOIA. This suit filed by KYNF/EDI/McCoy 8/8/06
has been dragged out by DOE apparently to ensure that these documents -
regardless of Downes' ruling - will remain unavailable for our ID District
Court ATR NEPA suit discussed above.
|
Meeting on Payette nuke plant
plan draws 400 Residents and Activists
Pose Tough Questions to the |
Rocky
Barker reports 12/21/07 in the Idaho
Statesman; “The developer of a proposed nuclear plant near Payette faced
tough questions about safety, traffic, water and future quality of life in his
first public meeting on Thursday.
Residents peppered Bill Fehrman,
president of MidAmerican Nuclear Energy Co., with questions colored by their
skepticism since learning about the plant proposed northeast of this lower
Treasure Valley city near the confluence of the Payette and Snake rivers.
Fehrman promised the restless crowd
of more than 400 people at Payette High School more answers as the company
moves closer to a decision on whether to build the plant, a decision it hopes
to make by next fall.
The big issue in this desert
agricultural community is water. "Where are we going to get the water when
even our farmers can't get enough?" asked Kurt Key, a Payette carpenter.
The reactor would use an estimated
25,000 acre-feet of water annually, more than a quarter of the water stored in
Lucky Peak Reservoir, Fehrman said. The company has several options for buying
it and is studying strategies to get the water at the least cost and without
hurting existing water users, he said.
Walt Bosse, a retired cement plant
supervisor, worries about what environmental safeguards the company will take.
"If they have a problem, they're going to flood the reactor," Bosse
said. "What are they going to do with that water?"
Fehrman said many of the details will
come later when the company decides what reactor it will use and after nearly a
year of studies planned even before the company decides to move forward. Then
the project will face a four-year review by the Nuclear Regulatory Commission,
which will look closely at environmental hazards. If MidAmerican decides to go
forward next year, it could be another 12 years before electricity is produced.
Not everyone was negative. Duane
Youngberg, who owns a heating and cooling business in Payette, said he was
excited about the economic potential the plant presents. And he wasn't worried
about the plant's safety.
Radiation, said Twin Falls
anti-nuclear activist Peter Rickards. He urged residents to push their
lawmakers to pass laws to stop the plant and was applauded by part of the crowd
when he said, "Let's not let it into Idaho."
Residents near the proposed site
expressed concerns about traffic and land values. Nicole and Phil Hyatt lost a
buyer for their home when the news of the plant became public Dec. 4.
One Payette native had waited for
years for this day to arrive. Former Sen. James McClure was one of nuclear
power's strongest advocates as chairman of the Senate Energy and Natural
Resource Committee. Now he is a consultant for MidAmerican. The current
assessed valuation of Payette County is just over $1 billion, he told the
crowd. A nuclear plant could add $8 billion to $10 billion in assessed value,
which could mean great economic benefits. "It's a very, very good deal for
Payette County," McClure said.
Tim Kennedy of New Plymouth was not
convinced. The plant site is one of his favorite hunting spots. He said he
worried about living downwind. "You'll see me on horseback with a protest
sign wherever you go," he said to a round of applause. But a few voices chimed in saying, "Speak
for yourself."
|
How Risky is the New Era of |
Paul Davidson reports in USA Today (12/11/07); “Nearly two years
ago, the Nuclear Regulatory Commission gave the operator of the Indian Point
nuclear plant a year to add backup power supplies to the plant's emergency
warning sirens. Entergy paid a $130,000 government fine in April — but still
hasn't done the work at the plant 24 miles north of New York City.
At the Peach Bottom nuclear plant
south of Harrisburg, Pa., security guards often took 15-minute "power
naps," according to a letter from a former security manager to the NRC
last March. The NRC began investigating after CBS News aired video of the
dozing guards in early September.
Neither of the incidents amounted to
an "immediate" safety risk, the NRC says. But they — and hundreds of
other seemingly minor episodes at nuclear power plants in recent years — are
drawing increased scrutiny as the USA prepares to launch a new generation of
nuclear reactors.
Since the 1979 Three Mile Island
accident, there have been 18 "significant precursors," or equipment
failures, at U.S. nuclear plants that sharply raise the chance of a reactor
core meltdown, says the Nuclear Regulatory Commission. There have been four
since 1990. Since 1988, there have been 337 precursors that increase the risk
of a meltdown more modestly. Problems
that increase the risk of a core meltdown within a year jumped from an average
1 in 17,000 to greater than 1 in 1,000. Power companies are beginning to file
applications to build up to 32 nuclear plants over the next 20 years, the first
since the 1979 accident at the Three Mile Island plant in Pennsylvania halted
plans for new reactors and led to sweeping changes in safety regulations. It's
partly a reflection of how, amid concerns about climate change, communities
have become more open to nuclear power as a cleaner alternative to pollution-belching
coal-fired plants.
An Ohio nuclear plant is being
allowed to reopen after a two-year shutdown over safety issues stemming from an
acid leak that ate through a protective steel reactor cap, the Nuclear
Regulatory Commission announced.
Nuclear plant told
to tighten safety measures
The government ordered an
Ohio utility company Thursday to take stricter safety measures at its
Davis-Besse nuclear power plant, which has been shut down for the past two
years. FirstEnergy, the plant's owner and operator, says it will
comply with the order and hopes to soon restart the reactor.
Critics and advocates of nuclear power
generally agree that improvements in equipment and employee training have
helped to make nuclear plants safer since the partial meltdown of a reactor at
Three Mile Island.
Watchdog groups, however, say that
unless nuclear safety and security improve, the USA's expansion of its nuclear
power industry — which now involves 104 reactors that supply about 20% of the
nation's electricity — could pose risks to nearby communities.
"Serious safety problems"
plague U.S. nuclear plants because the NRC isn't adequately enforcing its
standards and has cut back on inspections, according to a report released
Tuesday by the Union of Concerned Scientists (UCS), a nuclear safety watchdog
group.
The report also says that even
though security at nuclear plants was increased after the Sept. 11 terrorist
attacks, reactors still aren't sufficiently protected against terrorist threats
such as hijacked jets, and new reactors aren't being designed to be
significantly safer than existing ones. Increasing the number of reactors without
creating "unacceptably high safety and security risks" could be
difficult, the report concludes.
There has been no meltdown of a
reactor in the USA since the incident at Three Mile Island, which led to no
deaths or identifiable injuries from radiation exposure but resulted in the
release of some radiation from the plant.
However, since 1979, U.S. nuclear
plants have had to shut down 46 times for a year or more, in most cases to fix
equipment problems that accumulated over time and that regulators should have
ordered repaired earlier, according to the UCS, which compiled the data from
the NRC and other research. And the number of equipment failings that increase
the risk of an accident is up since 2001, compared with the previous five-year
period, NRC figures show.
The UCS says incidents such as
occasional failures of pumps that cool the nuclear reactor core in an emergency
eventually could prove disastrous if they coincide with other low-probability
events, such as coolant leakages from the core. "The track record on existing reactors
leaves much to be desired, and until you fix that problem, it's going to carry
over to new reactors," says David Lochbaum, director of UCS' nuclear
safety project.
The NRC says that in the episode involving
the sleeping guards at Peach Bottom, it didn't act sooner because it couldn't
substantiate the claims with Exelon the plant's operator. At Indian Point,
Entergy says its plan to install backup power for the sirens has been delayed
by technical hurdles and the need to get permits from dozens of towns, counties
and state offices.
“A Reliable Fleet of Reactors” ??
Nuclear reactors generate heat that
produces electricity when uranium atoms split. In the reactor core, uranium is
kept in water to prevent it from overheating, melting down and releasing
radiation. A meltdown by itself
typically would not be disastrous because the reactor sits in a concrete
containment structure to prevent radiation from escaping.
However, a meltdown could cause a
buildup of temperature and pressure that ruptures the containment building. A
massive release of radioactive gas into a surrounding community could destroy
or damage human cells and cause death or cancer. That's what happened at the
Chernobyl nuclear plant in the former Soviet Union in 1986. The world's worst
nuclear plant disaster involved a meltdown and an explosion that killed 56
people. At least an additional 4,000 are projected to die from cancer because
of exposure to radiation.
In the accident at Three Mile Island
seven years earlier, water cooling the core in one of the plant's two reactors
leaked through a partly open valve. The valve was closed enough to prevent an
alarm from sounding. Half the core melted, but the containment building stopped
all but a small amount of radiation from seeping into the environment.
The incident led the U.S. government
to require upgrades in piping, valves and other equipment at all nuclear
plants, and NRC inspections were increased.
Union of Concerned Scientists UCS' Lochbaum counters that the 46 reactor
shutdowns during the past three decades indicate there has been a buildup of
multiple problems that regulators should have caught sooner. In 1995, for
example, Public Service Electric & Gas had to close its Salem plant in New
Jersey for three years until 43 equipment problems were fixed, including a
broken fan that kept safety gear from overheating.
A Government Accountability Office
report said the NRC knew about 38 of the flaws — in two cases for more than six
years — and that its "lack of more aggressive action" compounded the
plant's problems.
Plants inspected less frequently
In the most serious episode
involving a U.S. nuclear plant since Three Mile Island, the Davis-Besse plant
in Ohio was shut down from 2002 to 2004 after the NRC failed to spot what it
acknowledges were early signs of trouble.
An acid leak through the reactor
vessel's lid left a quarter-inch-thick steel veneer, according to NRC reports.
Because emergency pumps also were faulty, core-cooling water leaking through
the ruptured lid could have led to a meltdown.
The NRC identified the leak in fall 2001 but let the plant keep
operating. An NRC Inspector General's report in 2002 found the agency's
willingness to keep the plant running "was driven in large part by a
desire to lessen the financial impact on (plant operator FirstEnergy) that
would result from an early shutdown."
In a statement last month, the NRC
blamed FirstEnergy for providing "inaccurate and misleading information,"
including its "explanation of the leak." FirstEnergy says it has made
extensive staffing and procedural changes to prevent such situations in the
future. Stuart Richards, deputy director of the NRC's inspection unit, says
such shutdowns show "that if the NRC feels plants shouldn't be operating,
we'll take appropriate actions."
NRC credits a more precise oversight
system, launched in 2000, that increases inspections at poorly performing
plants. However, one key safety measure — of problems that the NRC says
increase the annual risk of a meltdown from an average of 1 in 17,000 to up to
1 in 1,000 — has doubled the past six years to an average of 18 a year. There have been 337 such
"precursors" since 1988, including failures of pumps that supply water
to reactors in a crisis, the NRC says.
Half the problems stemmed from the
loss of power — needed to run critical cooling systems — and most of those
occurred during the massive electricity blackout that struck the northeastern
USA on Aug. 14, 2003. The other half involved cracks in nozzles that, in some
cases, let water seep from a reactor.
Lochbaum says that such
explanations by the NRC do not ease his concerns about plants' safety. He
blames the increasing "precursors" on scaled-back inspections by the
NRC and plant owners. From 1993 to 2000,
routine NRC inspection hours declined by 20%, partly because of budget
constraints, the NRC acknowledges.
Questions about standards
In its report, the Union of
Concerned Scientists (UCS) says the NRC has not consistently enforced many of
its safety regulations for nuclear plants.
The group says that since 1981, for example, the NRC has issued about
1,000 exemptions to plants that failed to meet fire-protection rules that went
into effect after a 1975 blaze at the Browns Ferry plant in Alabama.
The NRC says the waivers were granted
to older plants that couldn't make certain structural changes such as separating
primary and backup safety gear. Waivers permit alternative fire-prevention
methods, such as sprinklers or smoke alarms.
NRC Commissioner Gregory Jaczko says the agency should require plants to
take more elaborate steps, such as installing fire-resistant power cables as
backups to standard sets.
In February 2000, a steam generator tube
at the Indian Point plant ruptured, causing a small radiation leak outside the
plant. Workers had spotted corrosion in the tube in 1997, but Con Edison, the
plant's operator, persuaded the NRC to delay a follow-up inspection slated for
June 1999. An NRC engineer was skeptical of the request, but agency policy
discouraged her from asking follow-up questions, an NRC Inspector General's
report found later. The tube broke before the next scheduled inspection in
2000. The NRC says the inspection was delayed because the plant had been shut
down for 10 months before the request, leaving little time for the tube to
degrade further.
The UCS' Lochbaum largely blames
enforcement lapses on an NRC culture he says discourages workers from raising
safety issues out of fear of retaliation. A 2002 Inspector General's survey
said only 53% of NRC employees "feel it's safe to speak up" at the
agency.
|
Hanford Test Reactor Fuel Being
Sent to Idaho |
The Associated Press, Tri-City Herald
reports 1/7/08 “ Nuclear fuel from the
Fast Flux Test Facility at the Hanford nuclear reservation is being shipped to
Idaho to have the uranium extracted for possible reuse by commercial nuclear
power plants.
That's part of the work to shut down
the research reactor at minimum cost, according to the U.S. Department of
Energy. Despite years of efforts by FFTF supporters, the federal government has
been unable to find a cost-effective use for the research reactor.
"The sodium-bonded fuel is the
last remaining fuel at FFTF," said Al Farabee, the Department of Energy's
FFTF federal project director. The sodium-bonded fuel was a later design for
use in the reactor, which operated from 1982 to 1992. Melted sodium was poured
around the fuel pellets inside each fuel pin to conduct heat from plutonium and
uranium. The sodium bonded the pellet to the cladding.
The reactor also had 375 fuel
assemblies without sodium bonding. They have already been moved out of FFTF
into storage on the sprawling Hanford site.
Unused and irradiated sodium-bonded fuel is being shipped to Idaho in
steel and lead-shielded casks that are sealed airtight.
At the Idaho National Laboratory,
the fuel will be stored inside the Hot Fuel Examination Facility until it is
processed, beginning in fiscal year 2009, according to the Department of
Energy. Processing is expected to take two years.
Uranium will be extracted from the
fuel and cast into ingots, and will be stored until a customer is found, the
DOE said. At FFTF, all sodium used in the reactor's cooling systems has been
removed and is being stored onsite. The sodium, which includes radioactive
contamination, is expected to be used as a caustic additive to help turn radioactive
waste now stored in underground tanks at Hanford into a stable glass form.”
The Hot Fuel Examination Facility is located
at the Idaho National Laboratory Materials Fuel Complex formerly called
Argonne-West that uses electro-metallurgical Spent Nuclear Fuel reprocessing
also associated with the production of weapons grade fissile material (Pu &
HEU).
This process is in violation of the
Non-Proliferation Treaty that the Bush Administration now is denying.
|
Radiation
Sickened 36,500 and Killed at Least 4,000 of Those Who Built Bombs, Mined
Uranium, Breathed Test Fallout |
Ann Imse reports in the Rocky Mt. News 8/31.07 that; “The U.S.
nuclear weapons program has sickened 36,500 Americans and killed more than
4,000, the Rocky Mountain News has determined from government figures.
Those numbers reflect only people who have
been approved for government compensation. They include people who mined
uranium, built bombs and breathed dust from bomb tests.
Many of the bomb-builders, such as
those at the Rocky Flats plant near Denver, have never applied for compensation
or were rejected because they could not prove their work caused their
illnesses. Congressional hearings are in the works to review allegations of
unfairness and delays in the program for weapons workers.
The Rocky calculation appears
to be the first to compile the government's records on the human cost of
manufacturing 70,000 atomic bombs since 1945. It is based on compensation
figures from four federal programs run by the Departments of Labor, Justice and
Veterans Affairs. Many people have been paid only recently.
More than 15,000 of the 36,500 are
workers who made atomic weapons. They were exposed to radiation and toxic
chemicals that typically took years to trigger cancer or lung disease.
Others were civilians living near
the Nevada test site during above-ground nuclear tests; soldiers and workers at
test sites; and uranium miners and millers who breathed in radioactive dust
until 1972 when the government stopped buying uranium.
At least 4,000 of the 36,500 died.
This number reflects cases where survivors could be paid only if their relative
died of the covered illness.
Many more of the 36,500 likely also
have died of the deadly diseases triggered by their work. But in most of the
compensation programs, the government does not track deaths or cause of death,
so the true number who gave their lives to support the nuclear bomb program
probably will never be known.
Some were contaminated through
accident or ignorance. But government documents have revealed that officials at
times risked the health of civilians, soldiers and workers because they
believed national security demanded it. “
Web References
[1] KYNF
v. DOE, Idaho District Court, Case 4:07-cv-00036-BLW, Doc. No. 69, Errata to
December 3, 2007 Declaration of Robert D. Boston, DKT. No. 64.
[2] R. D. Boston Declaration in KYNF v. DOE , Administrative Record Doc. No. 64, 12/3/07, para. 25.
[3] KYNF
v. DOE, Civ. No. 07-36-E-BLW, Reply Memorandum of Points and Authorities in
Further Support of Plaintiffs’ Motion for Summary Judgment, 9/14/07. Also see EDI Newsletter Nov./Dec. 2007; and
ATR Risk Report available at;
http://environmental-defense-institute.org/
[4] DOE/ID
Facility Certification Report No. 29, “This certification is for the operation
of the Advanced Test Reactor (ATR) to be implemented during Cycle 134B-2 and
continuing with subsequent cycles under Technical Safety Requirement (TSR) 186,
Revision 14, April 7, 2005. Also cited
in Plaintiffs original NEPA Complaint, 1/10/07.
[5] Facility Certification Report No. 29, for
ATR,
[6] Document ID: SAR-153, Revision ID:16,
Effective date
[7] KYNF
v. DOE, Civ. No. 07-36-E-BLW, Administrative Record 006517. “Source Term” is
defined by DOE as “The quantity of radioactive material released by an accident
or operation that causes exposure after transmission or deposition. Specifically,
it is that fraction of respirable material at risk that is released to the
atmosphere from a specific location. The source term defines the initial
condition for subsequent dispersion and consequence evaluations.”
DOE/EIS-0287D, pg D-33
[8] KYNF v. DOE, Civ. No. 07-36-E-BLW, Administrative Record No. 006517.
[9] DOE/EIS-0287 pg. 4-30; DOE/DEIS-0373D, pg 3-26.
[10] D. McCoy, C. Broscious, “Unacceptable Risk at the INL the Case for ATR Closure, Revised 1/08.
[11] See EDI website http://environmental-defense-institute.org